When I picked up a Shilen ar15 barrel that was chambered in a 17 Remington, I was disappointed to find there was no brass that was reasonably priced.
Paying $1.10 per case was not what I wanted to do… if his Lapua or Atlas brass or Peterson brass in 17rem then I would pay.. but not for Nosler brass… that is essentially 204 Ruger necked down…
I started by converting 556 or 223 range brass into 17 Remington. It worked .. and as I perfected, it worked quite well and I could if I quickly and anealed between running the brass through the 17 Remington die could stretch the neck out almost to the regular length… but thinning the neck too much? I don’t think it was something that was good to do… the flipside I was turning the neck when they were short…
worrying about developing carbon.. and the fact that 204 Ruger brass actually became available once again and quite reasonable…
I had picked up a 204 Ruger shilen barrel for the ar15… ran out for a bit because I got tired of messing around with brass for the 17 Remington…
I decided on a whim to throw the 204 Ruger brass into the 17 Remington die to see what happens…
New brass didn’t work well not sure if it was too soft down the body, but after the brass was fired, it seemed to work better and didn’t crush… and didn’t develop the dimples around the neck or creases, depending on how bad it was this made some of them unusable because it extended too far up into the neck..
I had initially annealed the new cases prior to loading/firing… quite possibly the newer cases were too hard and crushed, and the other ones that were annealed, although fired, were still soft and allowed the brass to move inward without buckling.
Finally figured it out I used fired 204 Ruger brass once I got the neck down to 17 Remington and before pushing the shoulder back, I anealed the angled part of the case and the neck… I have a induction a dealer self-made so it can be real quick..
So when I do the final, push the shove the shoulder back no more dimples I’m ecstatic!!
The cases look great
I was going do a progression picture from when I first tried it to what they’re doing now, but I did not do it… behind the nice cases.. are the first few ones of the bad ones
After I get more done, I’ll set up my trim and trim them all at once… as right now they’re a bit too long and hit the lands
Unfortunately, my borescope does not go down a 17 caliber. You have to buy that really expensive one forgot the name of it.
Paying $1.10 per case was not what I wanted to do… if his Lapua or Atlas brass or Peterson brass in 17rem then I would pay.. but not for Nosler brass… that is essentially 204 Ruger necked down…
I started by converting 556 or 223 range brass into 17 Remington. It worked .. and as I perfected, it worked quite well and I could if I quickly and anealed between running the brass through the 17 Remington die could stretch the neck out almost to the regular length… but thinning the neck too much? I don’t think it was something that was good to do… the flipside I was turning the neck when they were short…
worrying about developing carbon.. and the fact that 204 Ruger brass actually became available once again and quite reasonable…
I had picked up a 204 Ruger shilen barrel for the ar15… ran out for a bit because I got tired of messing around with brass for the 17 Remington…
I decided on a whim to throw the 204 Ruger brass into the 17 Remington die to see what happens…
New brass didn’t work well not sure if it was too soft down the body, but after the brass was fired, it seemed to work better and didn’t crush… and didn’t develop the dimples around the neck or creases, depending on how bad it was this made some of them unusable because it extended too far up into the neck..
I had initially annealed the new cases prior to loading/firing… quite possibly the newer cases were too hard and crushed, and the other ones that were annealed, although fired, were still soft and allowed the brass to move inward without buckling.
Finally figured it out I used fired 204 Ruger brass once I got the neck down to 17 Remington and before pushing the shoulder back, I anealed the angled part of the case and the neck… I have a induction a dealer self-made so it can be real quick..
So when I do the final, push the shove the shoulder back no more dimples I’m ecstatic!!
The cases look great
I was going do a progression picture from when I first tried it to what they’re doing now, but I did not do it… behind the nice cases.. are the first few ones of the bad ones
After I get more done, I’ll set up my trim and trim them all at once… as right now they’re a bit too long and hit the lands
Unfortunately, my borescope does not go down a 17 caliber. You have to buy that really expensive one forgot the name of it.
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