I recently received a Mighty Armory .223 Gold Match sizing die. I currently use a Redding Type S bushing die and then mandrel size the cartridge neck. I'm hoping to use the MA die to reduce the two steps into one step. Based on all the reviews here I thought it would work well, but testing it out yesterday says otherwise. I'm using Lapua brass so that might be a factor since it is thicker than many other types of brass.
When sizing a piece of brass it easily sizes the neck and body on the press upstroke, but on the downstroke it requires quite a bit of effort to get the case back out of the die. Investigating this, I removed the mandrel and sized a piece of brass. The neck ID measures .214". The finish size with the mandrel installed is .221 which is exactly where I want it. Given this the mandrel has to size the neck ID from .214 to .221! That seems like too much sizing going on in the neck to me. Also seems like it is way overworking the brass. It also explains the amount of effort required on the downstroke with the mandrel installed. I've spoken to Wayne about it and apparently everything is dimensionally correct with the die. Has anyone else experienced this?
I'm thinking I need to machine the MA die neck bore to a larger size? With my Redding die I use a .245 bushing which results in a .219 neck ID. The final sizing operation with a separate mandrel die requires little effort and consistently results in a .221 neck ID.
When sizing a piece of brass it easily sizes the neck and body on the press upstroke, but on the downstroke it requires quite a bit of effort to get the case back out of the die. Investigating this, I removed the mandrel and sized a piece of brass. The neck ID measures .214". The finish size with the mandrel installed is .221 which is exactly where I want it. Given this the mandrel has to size the neck ID from .214 to .221! That seems like too much sizing going on in the neck to me. Also seems like it is way overworking the brass. It also explains the amount of effort required on the downstroke with the mandrel installed. I've spoken to Wayne about it and apparently everything is dimensionally correct with the die. Has anyone else experienced this?
I'm thinking I need to machine the MA die neck bore to a larger size? With my Redding die I use a .245 bushing which results in a .219 neck ID. The final sizing operation with a separate mandrel die requires little effort and consistently results in a .221 neck ID.