Inspired by the "What Were They Thinking" thread.
This is Robert. Don’t be like Robert...
This is a personal project so at least I’m not buying a customer a barrel. This barrel is 1.375 for 5” then tapering to 1.010” at 32” and I have a second one. Losing 1-1/4” on the chamber end isn’t really going to be the end of the world for me.
So, the threads were not too tight and the barrel had already been screwed on/off hand tight several times during the machining process. I knew it was going to be a while before I could finish this project so I washed the barrel and receiver with hot water and Dawn and dried. A little while later I was sitting in my office (probably after a few cocktails) looking at the barrel, receiver, bottom metal and stock. I figured I’d screw the barrel on by hand and toss it in the stock to see what it will look like. Well, the dry barrel screwed in just fine....until it didn’t. I heard squeak, and it got tight. Tried backing it off and it only went about 1/4 turn. I immediately soaked it with penetrating oil and tried to back it off again. No joy. I knew at this point the receiver would be destroyed if I tried to use tools to unscrew it. It was time to sacrifice a bit of barrel and hope the receiver is OK.
After the tenon was extracted, the receiver looked pretty good. Just one tiny nick on a thread. I ended up making a mock tenon from some 4130 bar I had and lapped the threads with some 800g alox lapping compound and now can't hardly tell anything happened.
Moral of the story, ALWAYS lube your threads!
Started with this.
Knowing the the receiver would be destroyed if I tried to use force to unthread it, I cut the barrel off with a band saw. I then made some t-nuts to fit the front of the knee mill. I don't think this slot is really meant for machining off of, but for this OP, it wasn't going to be an issue.
Getting it as vertical as I can, hoping the threads are pretty parallel to the outside features of the action.
I knew this Chinese boring head and mystery boring bars would come in handy some day...
Just the smallest spot of galling on the threads. This would have been much worse if I had used tools to try to remove the barrel.
Good as new, just a bit shorter.
This is Robert. Don’t be like Robert...
This is a personal project so at least I’m not buying a customer a barrel. This barrel is 1.375 for 5” then tapering to 1.010” at 32” and I have a second one. Losing 1-1/4” on the chamber end isn’t really going to be the end of the world for me.
So, the threads were not too tight and the barrel had already been screwed on/off hand tight several times during the machining process. I knew it was going to be a while before I could finish this project so I washed the barrel and receiver with hot water and Dawn and dried. A little while later I was sitting in my office (probably after a few cocktails) looking at the barrel, receiver, bottom metal and stock. I figured I’d screw the barrel on by hand and toss it in the stock to see what it will look like. Well, the dry barrel screwed in just fine....until it didn’t. I heard squeak, and it got tight. Tried backing it off and it only went about 1/4 turn. I immediately soaked it with penetrating oil and tried to back it off again. No joy. I knew at this point the receiver would be destroyed if I tried to use tools to unscrew it. It was time to sacrifice a bit of barrel and hope the receiver is OK.
After the tenon was extracted, the receiver looked pretty good. Just one tiny nick on a thread. I ended up making a mock tenon from some 4130 bar I had and lapped the threads with some 800g alox lapping compound and now can't hardly tell anything happened.
Moral of the story, ALWAYS lube your threads!
Started with this.
Knowing the the receiver would be destroyed if I tried to use force to unthread it, I cut the barrel off with a band saw. I then made some t-nuts to fit the front of the knee mill. I don't think this slot is really meant for machining off of, but for this OP, it wasn't going to be an issue.
Getting it as vertical as I can, hoping the threads are pretty parallel to the outside features of the action.
I knew this Chinese boring head and mystery boring bars would come in handy some day...
Just the smallest spot of galling on the threads. This would have been much worse if I had used tools to try to remove the barrel.
Good as new, just a bit shorter.
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